Haulin200sx, thanks for the reply.
The engine did not make it through our last race. It overheated 4 hours into the race... :-( Timing and everything looked good when we checked it before the race. We think it was the head gasket or a failed (shut) thermostat (most likely the head gasket). It was weird because we werent burning water and temps were pretty good, but that was probably the reason for our lose of power.
Good news is I picked up a JDM sentra SR20 engine. It should have the 9.5:1 CR so we should be good to go with our stock tune. I have some "tune" bins from Calum's old posts so I will probably tweek one of those in the future.
We still have the 10:1 CR block and head, but it will probably need some machine before use. In one lap the water temps went from 220 to 290F (pegged out) and the Oil hit 300F so we have a feeling the block and head may be a warped. We compression tested the engine and it was bad... 120, 60, 50, 80. We have a race in two weeks, but we will disassemble the blown engine after that.
Thank you for your help with all of this tuning though :-)
On a side note: I have a U12 SR20det in my b13 SE-R and am having a weird issue I cannot seem to fix. The car bucks and boggs very bad at low throttle and high rpm. When ever the throttle body fully close, the engine boggs pretty harshly. I have to roll off the throttle very very slowly to keep it from upsetting the car when on the track. The engine is a stock U12 with a T25 and 7 psi stock waste-gate pressure. It does have an Ebay FMIC kit (put on before me) with a HKS (real) bov. I am currently running a stock U12 tune that is returning good AFRs (a little rich but it is a stock tune).
I have checked the TPS sensor and the voltages are good and NDS is showing the closed throttle activation at the lowest voltage point. I also recirced the bov and put the real HKS bov on (the previous was a fake one). I am recircing the flow from just upstream of the throttle body to just upstream of the turbo inlet (but downstream of the MAF). I have done a vacuum test but couldnt find anything. The engine seems to hold 22 psi vacuum at idle which seems healthy. The only issue I can think of at this point is the tune. I am assuming that since it has much more piping due to the FMIC that this is causing the issue. Either that or the way the hks bov is working compared to a stock recirc valve.
Any Ideas?? I am going to try disconnecting the bov and see if that helps. Only issue is I do not want to run it like that for long.