Turns out it wasn't the AFPR. Car was just running really lean. Pulled the plugs again and the ground was white, while the electrode base ceramic was BLACK on half, and super clean white on the other. The base of the threads were also black with carbon.
Was on the phone with Calum and he had me raise the injector latency way up to like 1.1ms, which I thought would be too high, but he re-assured me it's okay. Then we walked the K value up to around 230 from 218, and then back down to around 200.
She's idling much better, back fires on DECEL while in neutral, which freaked me out at first. I've never had the car backfire so loud before, but it doesn't really bother me I guess. 3" exhaust, anyone?
Tomorrow (it's raining right now) I'm going to take it around the block and do some datalogging from 2K~4K at steady speeds, and send them off for analysis. If the car seems to run fine N/A around the block a few times, I plan on hooking the intercooler piping back up, and taking it around the block few times to see how she reacts. Got my fingers crossed that I may have finally nipped this in the butt.