So after we finished up with Dan's car an he was on his way I turned focus to my car. I took the bov back apart and applied some plumbers tape to the threads of the vac nipple and the adjustment bolt, I'm not 100% satisfied that the leak is gone, but its better then it was that's for sure.
We also hooked up the boost gauge and it makes about 9psi max but falls to about 7psi an stays there till redline. The car pulls really smooth an power comes on good, but I think there's a lot left on the table.
We also hooked up the boost gauge and it makes about 9psi max but falls to about 7psi an stays there till redline. The car pulls really smooth an power comes on good, but I think there's a lot left on the table.