Dynoed My NX2K yesterday!!!
Well let me give some preface before I put the results up. Im waiting for Scrildo to get off his ass and post the Videos.
1. I had over heating issues that I dealt with right before the Dyno. It was a leaky Hose due to the clamp not putting enough force on it. Fixed that right before the Dyno but it was still to hot to bleed it.
2. Scrildo kept telling my my exhaust sounded like it was leaking. I agreed because the Downpipe has no gasket in it at this point. But its not leaking. TODAY i looked around my wastegate and the actuall gasket is burnt up and leaking. I couldnt figure out why it sounded like it did until Five minutes ago (day after the dyno:rolleyes. Missing HP right there!
3. I havent checked the base timing on this car once. Just kinda lined the Dissy back up with the marks and left it. Were pretty sure it was sitting at 12deg base. But cant be 100% sure until I get the specs on the UR pulley timing marks. Anyway we advanced the timing a bit without even going into timing mode and gained 20whp right away! JWT's timing maps are REALLY REALLY safe.
4. I know cams dont really break in per say. But when they are new they dont have that smooth shiney lobe like ones that have been in the motor and ran a while. So thats drag aka lost hp until they break in. The cams were put in 2-3 days ago.
Results to come. Keep in mind my goal was only 400whp and theres alot of stuff that just got fixed,and or needs to be adjusted/fixed that hasnt been yet. Gotta scan the sheets. I dynoed on the wastegate spring, low boost (about 16-17psi), and high boost 21psi. All runs had 100octane in the tank. I dont have sheets of any runs but high boost sadly.
Setup:
W10 Avenir w/stock block and head
-RC 750cc Inj
-JWT Fuel rail
-Nismo FPR
-S4 cams
-Z32 maf (Blow through)
-JRC Front mount IC
-2" Hotside 2.5" Cold side
-Greddy TD05h-18g
-Stock Manny with ext Tial 38mm wastegate
-stock J pipe
- 3" Downpipe to 3" side pipe
-JWT ECU w/SAFC2 on top
-AEM Tru-boost
1. I had over heating issues that I dealt with right before the Dyno. It was a leaky Hose due to the clamp not putting enough force on it. Fixed that right before the Dyno but it was still to hot to bleed it.
2. Scrildo kept telling my my exhaust sounded like it was leaking. I agreed because the Downpipe has no gasket in it at this point. But its not leaking. TODAY i looked around my wastegate and the actuall gasket is burnt up and leaking. I couldnt figure out why it sounded like it did until Five minutes ago (day after the dyno:rolleyes. Missing HP right there!
3. I havent checked the base timing on this car once. Just kinda lined the Dissy back up with the marks and left it. Were pretty sure it was sitting at 12deg base. But cant be 100% sure until I get the specs on the UR pulley timing marks. Anyway we advanced the timing a bit without even going into timing mode and gained 20whp right away! JWT's timing maps are REALLY REALLY safe.
4. I know cams dont really break in per say. But when they are new they dont have that smooth shiney lobe like ones that have been in the motor and ran a while. So thats drag aka lost hp until they break in. The cams were put in 2-3 days ago.
Results to come. Keep in mind my goal was only 400whp and theres alot of stuff that just got fixed,and or needs to be adjusted/fixed that hasnt been yet. Gotta scan the sheets. I dynoed on the wastegate spring, low boost (about 16-17psi), and high boost 21psi. All runs had 100octane in the tank. I dont have sheets of any runs but high boost sadly.
Setup:
W10 Avenir w/stock block and head
-RC 750cc Inj
-JWT Fuel rail
-Nismo FPR
-S4 cams
-Z32 maf (Blow through)
-JRC Front mount IC
-2" Hotside 2.5" Cold side
-Greddy TD05h-18g
-Stock Manny with ext Tial 38mm wastegate
-stock J pipe
- 3" Downpipe to 3" side pipe
-JWT ECU w/SAFC2 on top
-AEM Tru-boost