Hey coheed i know you mentioned you kept popping couplers off. Usually when that happens its usualy a suspect of a boost leak as well. Make sure you have any and all leaks fixed. That leak i told you about at my bov that i found yeah it made a huge difference in my a/f.
Lets just say my car is running soooooo freakin good right now. I did a pull through 5th gear being i dont have 4th, It pulled soo hard but at about 5500-6k it started to go lean 12.4:1 so i let off. Below that it was running 11.8 or so. This was with the vac line to the afpr plugged and not connected to it. This is how i was having to run it before to get a solid 11.6:1 a/f ratio and it worked and compensated. I thought it was the tune. Apparently not.
I connected the vac line to afpr and did another run through 5th, PUlled like a mad dog all the way through with a solid a/f of 11.5:1 I could not do this before without it just going to 10:1 on the wideband and sputtering out flooding out. Im soo happy i got that bug taken care of so make sure you check your piping and maybe make some changes to smoothen things out
Lets just say my car is running soooooo freakin good right now. I did a pull through 5th gear being i dont have 4th, It pulled soo hard but at about 5500-6k it started to go lean 12.4:1 so i let off. Below that it was running 11.8 or so. This was with the vac line to the afpr plugged and not connected to it. This is how i was having to run it before to get a solid 11.6:1 a/f ratio and it worked and compensated. I thought it was the tune. Apparently not.
I connected the vac line to afpr and did another run through 5th, PUlled like a mad dog all the way through with a solid a/f of 11.5:1 I could not do this before without it just going to 10:1 on the wideband and sputtering out flooding out. Im soo happy i got that bug taken care of so make sure you check your piping and maybe make some changes to smoothen things out