Go Figure, Building Boost Issues...
Witts end...
Okay, you guys are smarter than I am... There has to be something that I'm missing... here is the rundown. Car was boostin' like a son of a bitch on Saturday and Sunday... Sunday Night boost started to windle down. We fixed it on Monday by checking for leaks and tightening everything up, back to business! then slowly it started to windle down again. There is boost pressure, but it only builds to atmospheric (0psi gauge pressure). It basically drives like a strong n/a car, but when I let off the gas I can hear the turbo spool down every time.
Turbo is a gtir-t28 I bought about a year ago from a member, it was directly from a GTIR and has about 40k miles on it. It's actually in really good condition. Any questions, feel free to ask!
Things I have tried:
1) Boost Controller - I am running a Greddy Profec B (The old school one, I love it). When the car was boosting fine it actually did its job, very well I might add. There was speculation that the diaphram was leaking on it. So i removed it completely from the system. Took the lines off the tee on my compressor housing, and took the line off of the wastegate actuator. I then put a new line directly from the compressor housing tee to the wastegate. Same thing. Not the issue.
2) Wastegate Actuator being stuck open - This was my first notion... I actually was using a forge adjustable actuator, has multiple springs. I've replaced the 10-14lb spring with the 14-18lb spring - same issue, I removed the arm and tightened it to apply more preload, twice - same issue. I removed this actuator and put on the stock GTIR actuator again, added preload twice again - same issue. Lastly, I ran the car with no pressure source line to each wastegate - same issue. It's not the actuator.
3) Large Vacuum/Boost Leaks - I went up to a friends house on Monday and pressure tested. There were a couple of small leaks. I took off my intake piping and actually clamped the compressor directly to the turbo inlet, after popping off the actual tester a couple times, lol... it held 20-23 psi no problems. We basically tightened the bov to the piping, and the top hat on the bov down, and tightened the spring. The car pulled like a beast when we took it out. It held 9lbs w/ th eboost controller off, and i turned it up to 12lb for a second and it did AWESOME. Then I let Brennan drive it and he said it was only holding 7ish pounds... As I was driving home, 4lb, and eventually 0. And now its acting the same exact way it was before I drove over there... Idles fine, but doesn't build boost over atmospheric. I've looked the car up and down, and I can't find any leaks... I will have to pressure test again this weekend.
4) Turbo Being Fubarred or unbolting itself from heat - The turbo has no outrageous shaft play, spins freely, and is not scraping the housing walls anywhere. The wastegate flapper works fine, and all housings are tight. I even went through and tightened all the housing bolts after the first couple of days. I checked all the bolts to the turbine inlet to manifold and they are tight. The exhaust manifold seems to be seated to the head well, I went over and retightened them. The turbo doesn't spit any black, or white, or rainbow colored smoke. I can hear the turbo spool down after any amount of throttle. I'm going to put exhaust on the car so I can hear everything a little better this weekend.
5) Leaking B.O.V. - I am running a Blitz SS blow off valve w/ a recirc fitting recirced post maf. It boggles my mind because it held the boost on the previous pressure test? I don't see why or how this could be the problem, but after ranting and complaining to my friend, its the only thing at this point that makes sense (Good vac, boost leaking somehow). After I got home on Monday and the pressure stopped building, I tightened the spring down as far as it could go and still the same thing. Could the diaphram be stuck open? That might explain why I can't build boost... I will take it off tonight and check it.
Other random Facts:
- The spark plugs look great, BKR7E from NGK. They were what were in the car when I put her down in November 2007.
- Vacuum is good and pulls around 17inHG at idle. Under load in gear letting th eengine slow the car, well past 25inHG
- I set my TPS at .4 close and 4.00v at wot on Tuesday. (I noticed it was around .54v closed and 5.4 or so wot)
- I set my timing at 15 degrees on monday... I guess I could set it again since I reset the TPS, but it shouldn't matter since its done with the TPS unplugged.
- At the moment running a 4bar 370 program w/ a gtir MAF, just like my sentra. Computer is fine. MAF readings work
- Battery was moved to the rear, Voltage is 12.0-12.4v car off no accessories, when running I see 14.1v.
- Everything electrical is verified by Nissan Data Scan
- IACV/AAC is working from what data scan says...
- I'm using ALL t-bolt clamps and fresh couplers from silicone intakes dot com, and everything is tight.
The only thing I can think of at this point is that I sprung another leak somewhere, but it doesn't make sense because my vacuum is all good. What in the hell is going on here? I'm going to see if I can run another pressure test. i really want to get this car on the road again and healthy before I put her down for the winter so I can do my upgrades that are sitting on the shelf
Anything and everything will help... I'm all ears, and I will do anything. Any questions please feel free to post them up. I have exhausted my brain trying to figure this one out. Usually these issues are all stupid simple fixes, but this one is kicking my ass.
Tokes
Okay, you guys are smarter than I am... There has to be something that I'm missing... here is the rundown. Car was boostin' like a son of a bitch on Saturday and Sunday... Sunday Night boost started to windle down. We fixed it on Monday by checking for leaks and tightening everything up, back to business! then slowly it started to windle down again. There is boost pressure, but it only builds to atmospheric (0psi gauge pressure). It basically drives like a strong n/a car, but when I let off the gas I can hear the turbo spool down every time.
Turbo is a gtir-t28 I bought about a year ago from a member, it was directly from a GTIR and has about 40k miles on it. It's actually in really good condition. Any questions, feel free to ask!
Things I have tried:
1) Boost Controller - I am running a Greddy Profec B (The old school one, I love it). When the car was boosting fine it actually did its job, very well I might add. There was speculation that the diaphram was leaking on it. So i removed it completely from the system. Took the lines off the tee on my compressor housing, and took the line off of the wastegate actuator. I then put a new line directly from the compressor housing tee to the wastegate. Same thing. Not the issue.
2) Wastegate Actuator being stuck open - This was my first notion... I actually was using a forge adjustable actuator, has multiple springs. I've replaced the 10-14lb spring with the 14-18lb spring - same issue, I removed the arm and tightened it to apply more preload, twice - same issue. I removed this actuator and put on the stock GTIR actuator again, added preload twice again - same issue. Lastly, I ran the car with no pressure source line to each wastegate - same issue. It's not the actuator.
3) Large Vacuum/Boost Leaks - I went up to a friends house on Monday and pressure tested. There were a couple of small leaks. I took off my intake piping and actually clamped the compressor directly to the turbo inlet, after popping off the actual tester a couple times, lol... it held 20-23 psi no problems. We basically tightened the bov to the piping, and the top hat on the bov down, and tightened the spring. The car pulled like a beast when we took it out. It held 9lbs w/ th eboost controller off, and i turned it up to 12lb for a second and it did AWESOME. Then I let Brennan drive it and he said it was only holding 7ish pounds... As I was driving home, 4lb, and eventually 0. And now its acting the same exact way it was before I drove over there... Idles fine, but doesn't build boost over atmospheric. I've looked the car up and down, and I can't find any leaks... I will have to pressure test again this weekend.
4) Turbo Being Fubarred or unbolting itself from heat - The turbo has no outrageous shaft play, spins freely, and is not scraping the housing walls anywhere. The wastegate flapper works fine, and all housings are tight. I even went through and tightened all the housing bolts after the first couple of days. I checked all the bolts to the turbine inlet to manifold and they are tight. The exhaust manifold seems to be seated to the head well, I went over and retightened them. The turbo doesn't spit any black, or white, or rainbow colored smoke. I can hear the turbo spool down after any amount of throttle. I'm going to put exhaust on the car so I can hear everything a little better this weekend.
5) Leaking B.O.V. - I am running a Blitz SS blow off valve w/ a recirc fitting recirced post maf. It boggles my mind because it held the boost on the previous pressure test? I don't see why or how this could be the problem, but after ranting and complaining to my friend, its the only thing at this point that makes sense (Good vac, boost leaking somehow). After I got home on Monday and the pressure stopped building, I tightened the spring down as far as it could go and still the same thing. Could the diaphram be stuck open? That might explain why I can't build boost... I will take it off tonight and check it.
Other random Facts:
- The spark plugs look great, BKR7E from NGK. They were what were in the car when I put her down in November 2007.
- Vacuum is good and pulls around 17inHG at idle. Under load in gear letting th eengine slow the car, well past 25inHG
- I set my TPS at .4 close and 4.00v at wot on Tuesday. (I noticed it was around .54v closed and 5.4 or so wot)
- I set my timing at 15 degrees on monday... I guess I could set it again since I reset the TPS, but it shouldn't matter since its done with the TPS unplugged.
- At the moment running a 4bar 370 program w/ a gtir MAF, just like my sentra. Computer is fine. MAF readings work
- Battery was moved to the rear, Voltage is 12.0-12.4v car off no accessories, when running I see 14.1v.
- Everything electrical is verified by Nissan Data Scan
- IACV/AAC is working from what data scan says...
- I'm using ALL t-bolt clamps and fresh couplers from silicone intakes dot com, and everything is tight.
The only thing I can think of at this point is that I sprung another leak somewhere, but it doesn't make sense because my vacuum is all good. What in the hell is going on here? I'm going to see if I can run another pressure test. i really want to get this car on the road again and healthy before I put her down for the winter so I can do my upgrades that are sitting on the shelf
Anything and everything will help... I'm all ears, and I will do anything. Any questions please feel free to post them up. I have exhausted my brain trying to figure this one out. Usually these issues are all stupid simple fixes, but this one is kicking my ass.
Tokes