.....
Didn't get a chance to dyno with it. I loaded the converted bin onto his ecu and tried to play with that but He wasn't making any numbers at all. His best was 160whp so we don't know what was wrong with his motor. Check cam timing and it was spot on, check compression and it was ok #1 was the lowest. Did have a bitch of a time trying to adjust the fuel on his @ idle. Not fiddling with the K is a pain lol. I tried to change injector size like you said and it was just crazy. It seemed to be just right for the WOT but the idle A/F was doing some funky stuff. I thought I could transition from the Nistune to the Nemu software. It was a big negative lol. We have to figure out what else is going on with the car 1st because It was just too quiet for N1 cams and peaked way too early.