Update!
Well, I pulled the head off and found that it was indeed warped past the limits outlined in the service manual. So I cut the mess out of it!!!
I ended up milling .030" off the head. I reinstalled and it didn't like that very much. Ran very poorly. Put in a call to my resident SR expert (Thanks Eric96Ser!) and he put me onto a set of adjustable cam gears. An hour or so later we're back running in tip top shape!!
I'm not sure if it's a placebo effect, but it seems like it revs quicker with more authority now..... Haven't driven it yet to see if there's a definitive power difference.
Next up is a way to tune this sucker and to stick it on my dyno!