Originally Posted by
Re-spect Thank You, Finally!!!! Like I said Strat, let the rest of them figure it out , we laid out the legwork. We can never say to ourselves that we never tried, and not once, but multiple times. Like all projects, and this is way beyond any other project,we tried and now its time for these other guys to shine. We will be known as the forefathers in the 2.4 game.....
your right fiz.
id like to give a last update pertaining to the last failure.
i dont know exactly why it failed but this is what failed.
i had the motor running for 700-1000 miles prior to failure.
it made 260 give or take on the dyno. felt great.
on the way home it poped around 7-8k during a wot pull in third.
hole the block in the front and also in the back.
the rod broke above the big end and the big end was still attached to the crank.
the broken rods bearing was shot and so was one of the other rod bearings that also destroyed the journal of the inside of the big end.
with that being said the crank had two bad journals.
the broken rod managed to hit the bottom of the #3 piston and put a good gash/dent in it.
the head luckily was unharmed.
i dont know what failed, all other bearings appeared to look good. the motor also seemed to need water in the radiator regularly. a little here and there but it comp tested and leak down test checked out. temps jumped up during break in, to about 220ish and dropped back down, that never happend agian. it ran very cool and even cooler on the dyno due to the e85's cooling properties.
so thats it in a nut shell.
ill build another ve. thats for sure. not sure what direction or when, as of right now im looking foward to just romping on the car and enjoying a reliable set up.
picking up a ve this weekend !
stratton.