Emergency Downpipe repair on a Supra. DP cracked while street tuning for one of my boys. HTP Invertig 131 DC @ 35A, HTP 55 cu ft, argon @ 19cfh 1/16" lanathated tungsten, .040 308L rods, did not backpurge or use solar flux
but I cleaned the gunk out of it with decarbonizer, soap, water, 600grit wet sand paper...lol forgot the 3m scratch pad.
Previous fabricator had merged dumptube with a cheapy flex section to dp which failed and had forced vbands together causing leak after downpipe, had to pie cut in 2 pieces to rotate and clock angle for no tension.
Re-did dumptube to atmosphere dump.
After that had to modify InlinePro S2K turbo kit w/ Invidia test pipe section. Using GReddy TiC exhaust with resonator delete, had to utilize 3 bolt home base flange, customer refused to change flanges.
3.0" 2 bolt off dp, used 2.75" section of pipe and welded on to 2.5" test pipe section. Realized 02 sensor clocked wrong contacting floor pan, noted exhaust resonator delete was welded at a slight angle causing exhaust to pull down with test pipe contacting GTSpec rear lower brace clocked it, tacked on car, welded off car.