So I got a chance to go get on it today, it was tryin to hit almost 15 psi and the boost needle was really jumpy, so i turned the mbc all the way out but its still runnin like 12psi, which is ok but the spring is only a 9lb lol
I think the bouncey boost needle was due to that janky ass coupler i had coming right off the turbo..
This one..
good thing when i was test fitting i knew i'd need a new coupler and ordered one, ebay for the win only took a few days and it had arrived at my friends, we didnt even know it was there an we were talkin about how it might be leaking an shit an his boy calls up at the shop an is like hey you got some funky blue hose thing in the mail, we were like WHOO HOO! cause we wernt expecting it till next week lol.
anyway heres the new one
had to trim about in inch off the 2.0" side, no biggy tho it fits great now
little top shot
you can see how its a tight fit, but whats new lol
I didnt notice the boost needle moving at all after the coupler change, it seemed steady, but still holding 12psi.. i think i'll take the mbc out an see how it does with out it..
I made a few virtual dyno runs, i dont know what to think, 2 of em are in the 320hp+ range and 270-280tq.. but that was with the boost leak or whatever.. i'll do some more runs soon an do a comparison to the one i made recently before the manifold swap.