Hesitation issue - need help!
Ok all you turbo junkies, I've got an issue I've been battling with for quite a while now, and I need some fresh advise!
The setup:
2001 Sentra SE - The motor started life as a stock roller rocker sr20 that came with the car. It's gone through a few iterations, but here's what's current with the motor:
protech log manifold
GT2871r w/T3 0.48a/r turbine housing
protech 3" dp that ends with a 16" resonator and turn down right behind the driver's seat
50lb injectors
jwt b14 ecu
fmic setup
z32 maf (blow thru setup)
emanage ultimate
eagle rods
cp 8.5:1 pistons
ARP head studs (done before reading all the bad stuff about them... :o )
stock head gasket (cometic didn't seal, didnt have time for machine work prior to a national prosolo event)
head is completely stock
innovate LM-1 afr tied into EMU for datalogging
Crane HI-6 ignition box
Crane LX-91 ignition coil (modified distributor cap for external coil)
plugs gapped to 0.028
fresh oem wires, cap and rotor
The problem:
When the car is at about 13psi or less, it runs perfectly. It pulls even and strong to redline. Above 13psi, I start to get a hesitation between 6100 and 6400 rpm. At 13.5-14psi, it basically feels like I lift a little, and then it pulls strong for the last couple hundred rpm. If I try to run 15psi, it will pull very hard up to 6100, and then it feels like I hit a rev limiter.
At first, I thought it was detonation. The car was originally on the stock b15 ecu with the EMU. I used the EMU to retard timing and control the injectors. I pulled more timing using the EMU. At one point, the car was downright sluggish. EGTs were higher, and the hesitation was still there. Hmmm, not it...?
Next I went to the plugs. I'm running ngk bkr7's. I closed the gap all the way down to 0.024. No change, but it idled rougher!
Ignition didn't seem to be the issue, unless the coil was failing, so I moved on to fuel issues. Throughout this whole process, I have been logging with the EMU. There were no visible issues with the injector duties, afr, timing, tps, or maf voltage. Could the injectors be failing at a specific duty cycle? Luckily, a local peformance shop (J Tune in Delaware) are a bunch of great guys. I was able to test a set of used injectors they had in the shop. I swapped, retuned the fuel maps, and gave it another go at 15psi. No change. Grrr.
Still not convinced it's not detonation, I stopped by a local sunoco after an autox. The tank was nearly empty, and they have 100 octane at the pump. After my most expensive tank of fuel in this car... no change. The hesitation happened in the exact same rpm range and boost. I would have expected it to at least shift with an octane increase, if it was detonation. Grrrrr.
My injectors back in, I decided it was time to step up my engine management game. I found a good deal on an obd II b14 jwt ecu and z32 maf, and now the car is running a jwt 8.5:1 compression, z32 maf, 72lbs msd tune. Since I have 50lb injectors, I used the EMU to tune the afrs (adjusted injector pulse, not maf voltage). I'm using the b15 intake still, so the iacv-aacv doesn't work. I have the idle up at 1100rpm to keep it from stalling when the fans turn on... with the loud exhaust it makes for fun looks at redlights Eventually I'll complete the mani swap and probably go to a realtime tuneable setup so I can ditch the EMU. Anyway, after all that, running on a completely new ecu program with better timing maps... the problem was still there. Grrrrrrr.
Back to the ignition. Could the coil be failing? I already had a Crane HI-6 ignition controller to help ease the redline bashing of autox (stock fuel cut was very harsh on the b15 ecu), so I added the complimenting LX-91 coil and modified the distributor cap. Note, by now I had also replaced the cap, rotor, wires, and plugs to see if they were the culprit. Again, after all that, no change. GRRRR.
So here I am. I've gone through fuel, ignition, overall ecu control, multiple variants on tuning with the EMU (used the built in injector scaling and manually adjusted fuel trims to compensate for injector sizes). What am I missing?
Could it be that the 0.48 T3 housing is too small and causing reversion issues with the stock cams and log manifold? There's no evidence of boost falling off. I'd hate to drop $300 on a larger T3 housing and still have the problem, but I can't think of anything else.
If anyone has a thought, please throw it out there. I may have forgotten a few things I tried, but I'm open to anything (preferrably things that don't take much $$ if we're not sure it is the issue). I've already thrown a lot of money at it in the above process, and I hate to keep doing it. Granted this was over quite a few months, but I have a feeling there's something simple I'm missing. Help me find it!!! Thanks in advance!
The setup:
2001 Sentra SE - The motor started life as a stock roller rocker sr20 that came with the car. It's gone through a few iterations, but here's what's current with the motor:
protech log manifold
GT2871r w/T3 0.48a/r turbine housing
protech 3" dp that ends with a 16" resonator and turn down right behind the driver's seat
50lb injectors
jwt b14 ecu
fmic setup
z32 maf (blow thru setup)
emanage ultimate
eagle rods
cp 8.5:1 pistons
ARP head studs (done before reading all the bad stuff about them... :o )
stock head gasket (cometic didn't seal, didnt have time for machine work prior to a national prosolo event)
head is completely stock
innovate LM-1 afr tied into EMU for datalogging
Crane HI-6 ignition box
Crane LX-91 ignition coil (modified distributor cap for external coil)
plugs gapped to 0.028
fresh oem wires, cap and rotor
The problem:
When the car is at about 13psi or less, it runs perfectly. It pulls even and strong to redline. Above 13psi, I start to get a hesitation between 6100 and 6400 rpm. At 13.5-14psi, it basically feels like I lift a little, and then it pulls strong for the last couple hundred rpm. If I try to run 15psi, it will pull very hard up to 6100, and then it feels like I hit a rev limiter.
At first, I thought it was detonation. The car was originally on the stock b15 ecu with the EMU. I used the EMU to retard timing and control the injectors. I pulled more timing using the EMU. At one point, the car was downright sluggish. EGTs were higher, and the hesitation was still there. Hmmm, not it...?
Next I went to the plugs. I'm running ngk bkr7's. I closed the gap all the way down to 0.024. No change, but it idled rougher!
Ignition didn't seem to be the issue, unless the coil was failing, so I moved on to fuel issues. Throughout this whole process, I have been logging with the EMU. There were no visible issues with the injector duties, afr, timing, tps, or maf voltage. Could the injectors be failing at a specific duty cycle? Luckily, a local peformance shop (J Tune in Delaware) are a bunch of great guys. I was able to test a set of used injectors they had in the shop. I swapped, retuned the fuel maps, and gave it another go at 15psi. No change. Grrr.
Still not convinced it's not detonation, I stopped by a local sunoco after an autox. The tank was nearly empty, and they have 100 octane at the pump. After my most expensive tank of fuel in this car... no change. The hesitation happened in the exact same rpm range and boost. I would have expected it to at least shift with an octane increase, if it was detonation. Grrrrr.
My injectors back in, I decided it was time to step up my engine management game. I found a good deal on an obd II b14 jwt ecu and z32 maf, and now the car is running a jwt 8.5:1 compression, z32 maf, 72lbs msd tune. Since I have 50lb injectors, I used the EMU to tune the afrs (adjusted injector pulse, not maf voltage). I'm using the b15 intake still, so the iacv-aacv doesn't work. I have the idle up at 1100rpm to keep it from stalling when the fans turn on... with the loud exhaust it makes for fun looks at redlights Eventually I'll complete the mani swap and probably go to a realtime tuneable setup so I can ditch the EMU. Anyway, after all that, running on a completely new ecu program with better timing maps... the problem was still there. Grrrrrrr.
Back to the ignition. Could the coil be failing? I already had a Crane HI-6 ignition controller to help ease the redline bashing of autox (stock fuel cut was very harsh on the b15 ecu), so I added the complimenting LX-91 coil and modified the distributor cap. Note, by now I had also replaced the cap, rotor, wires, and plugs to see if they were the culprit. Again, after all that, no change. GRRRR.
So here I am. I've gone through fuel, ignition, overall ecu control, multiple variants on tuning with the EMU (used the built in injector scaling and manually adjusted fuel trims to compensate for injector sizes). What am I missing?
Could it be that the 0.48 T3 housing is too small and causing reversion issues with the stock cams and log manifold? There's no evidence of boost falling off. I'd hate to drop $300 on a larger T3 housing and still have the problem, but I can't think of anything else.
If anyone has a thought, please throw it out there. I may have forgotten a few things I tried, but I'm open to anything (preferrably things that don't take much $$ if we're not sure it is the issue). I've already thrown a lot of money at it in the above process, and I hate to keep doing it. Granted this was over quite a few months, but I have a feeling there's something simple I'm missing. Help me find it!!! Thanks in advance!